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LAW OFFICE OF KARA E, GRANT <br />RK 15528 <br />Page 3 <br />TRAFFICFiRANSPORTATION REVIEW <br />The traffic study only reviewed weekday {7-9 am and 4-6 pm} traffic conditions. <br />Express Car Washes actually have their peak traffic generation on Saturdays at <br />approximately 1:00 pm or 2:00 pm. Also, the commercial area around the site <br />would have significant traffic conditions on a Saturday. Therefore, the traffic study <br />needs to perform a Saturday traffic analysis and utilize typical trip generation for an <br />Express Car Wash during those timeframes. RK has collected substantial trip <br />generation data for Express Car Washes in Santa Ana which are shown in the <br />attached Table 4-1. The Saturday trip generation is 50% higher on Saturdays than <br />during the weekday conditions. Therefore, a Saturday traffic analysis is required. <br />2. The near -term traffic conditions evaluation in the revised traffic study was for the <br />Year 2019- This is not a realistic timeframe, since it is nearly the last quarter of Year <br />2019. Since the project has not yet been approved and would need a period for <br />construction, a much later time -frame needs to be evaluated for near -term <br />conditions. An Opening Year of 2020 or 2021 is more realistic. <br />3. The traffic study took a trip credit for the traffic from the existing sit-down <br />restaurant building that is on the site at 301 North Tustin Avenue. This would only <br />be valid if the restaurant was in full operation when the traffic counts were taken. <br />The restaurant is currently closed. This needs to be verified and the trip credit cannot <br />be utilized if new traffic counts are taken to reflect 2419 conditions. <br />4. The site plan shown on page 3-68 (Figure 2-2) includes a full driveway access on <br />North Tustin Avenue. This driveway is located approximately 240-feet from the <br />intersection of Tustin Avenue at 41" Street. This distance appears to be too close to <br />allow this driveway to be a full service access with all turning movements, since it <br />would interfere with the northbound left turn pocket on Tustin Avenue. <br />5. The traffic counts mentioned on page 3-72 were taken in October of 2016, The <br />revised traffic study was prepared in 2019; therefore, it has been three years since <br />the traffic counts were taken in 2016, The traffic study should have been updated <br />with more current traffic counts in 2019 to reflect existing conditions. <br />6, There is no explanation on what the existing project "re-route" was for as shown on <br />page 3-73 and 3-74 (Figures 3-2 and 3-3). What has caused the re-route of traffic? <br />f'ft� amirreering <br />WW��hh33 enu0. �c. <br />75A-69 <br />